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ORNL/TM-2009/021
Effect of Intake Air Filter Condition on
Vehicle Fuel Economy
February 2009
Prepared by
Kevin Norman
Shean Huff
Brian West
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ORNL/TM-2009/021
Energy and Transportation Science Division
EFFECT OF INTAKE AIR FILTER CONDITION ON
VEHICLE FUEL ECONOMY
Kevin Norman
Shean Huff
Brian West
Date Published: February 2009
Prepared by
OAK RIDGE NATIONAL LABORATORY
Oak Ridge, Tennessee 37831-6283
managed by
UT-BATTELLE, LLC
for the
U.S. DEPARTMENT OF ENERGY
under contract DE-AC05-00OR22725
CONTENTS
Page
LIST OF FIGURES .................................................................................................................................. v
ACRONYMS AND DEFINITIONS ........................................................................................................ vii
ACKNOWLEDGEMENTS ...................................................................................................................... ix
1.INTRODUCTION AND BACKGROUND ....................................................................................... 1
2.EXPERIMENTAL SETUP ................................................................................................................ 3
2.1TEST FACILITIES ................................................................................................................... 3
2.2TEST SETUP ............................................................................................................................ 3
2.3DEFINING A CLOGGED AIR FILTER .................................................................................. 5
2.4VEHICLE TESTING ................................................................................................................ 6
3.RESULTS AND DISCUSSION......................................................................................................... 9
3.1MODERN VEHICLES ............................................................................................................. 9
3.1.1Initial Testing ............................................................................................................... 9
3.1.2WOT Testing ............................................................................................................... 9
3.1.3Performance and Fuel Economy .................................................................................. 14
3.2CARBURETED VEHICLE—1972 PONTIAC GRANDVILLE ............................................. 16
3.3FURTHER INVESTIGATIONS—SIMULATING A SEVERELY
CLOGGED FILTER ................................................................................................................ 19
3.3.11972 Pontiac Grandville .............................................................................................. 19
3.3.22007 Buick Lucerne ..................................................................................................... 23
4.CONCLUSIONS AND FUTURE WORK ......................................................................................... 25
4.1CONCLUSIONS ....................................................................................................................... 25
4.2FUTURE WORK ...................................................................................................................... 25
5.REFERENCES ................................................................................................................................... 27
iii
LIST OF FIGURES
Figure Page
2.1. Pressure transducer setup for modern vehicles. ........................................................................ 4
2.2. Air filter indicator. ..................................................................................................................... 4
2.3. 2007 Buick Lucerne filter restriction ........................................................................................ 7
2.4. 2007 Buick Lucerne filter restriction ........................................................................................ 7
2.5. 1972 Pontiac Grandville air filter .............................................................................................. 8
3.1. Maximum Outlet DP for 2007 Buick Lucerne baselined clean air filters ................................. 9
3.2. Newer vehicles tested ................................................................................................................ 10
3.3. Average maximum Outlet DP for the 2003 Toyota Camry during
the CRC E-60 WOT tests. ......................................................................................................... 11
3.4. Average Outlet DP at 3000 RPM during the CRC E-60 WOT tests. ........................................ 11
3.5. Average maximum Outlet DP for SS WOT tests. ..................................................................... 12
3.6. Air filter damage from WOT testing 2006 Dodge Charger ...................................................... 13
3.7. Acceleration time for CRC E-60 WOT tests ............................................................................. 13
3.8. Fuel economy for 2003 Toyota Camry ..................................................................................... 14
3.9. Fuel economy for 2007 Buick Lucerne ..................................................................................... 15
3.10. Fuel economy for 2006 Dodge Charger ..................................................................................... 15
3.11. 1972 Pontiac Grandville. ............................................................................................................ 16
3.12. Pressure port location for 1972 Pontiac Grandville. .................................................................. 16
3.13. Outlet DP for 1972 Pontiac Grandville during CRC E-60 WOT. .............................................. 17
3.14. Outlet DP for 1972 Pontiac Grandville during SS WOT. .......................................................... 18
3.15. Acceleration time for 1972 Pontiac Grandville during WOT tests ............................................ 18
3.16. Fuel economy for 1972 Pontiac Grandville ................................................................................ 19
3.17. Air filter average Outlet DPs for 1972 Pontiac Grandville during double HFET. ..................... 20
3.18. Damaged air filter from severely clogged air filter testing, 1972 Pontiac Grandville. .............. 20
3.19. FTP fuel economy for 1972 Pontiac Grandville. ........................................................................ 21
3.20. HFET fuel economy for 1972 Pontiac Grandville. .................................................................... 21
3.21. Average double HFET lambda for 1972 Pontiac Grandville. .................................................... 22
3.22. Damaged air filter from severely clogged air filter testing, 2007 Buick Lucerne. ..................... 23
3.23. Air filter average double HFET Outlet DP for 2007 Buick Lucerne. ........................................ 24
3.24. Severely clogged air filter fuel economy for 2007 Buick Lucerne. ........................................... 24
v
ACRONYMS AND DEFINITIONS
AFR air : fuel ratio
CRC Coordinating Research Council
DOE U.S. Department of Energy
DP pressure differential
ECE Economic Commission for Europe (used in referring
to driving cycles: ECE 15)
EPA U.S. Environmental Protection Agency
FEERC Fuels, Engines, and Emissions Research Center
(ORNL)
FTP Federal Test Procedure (EPA)
HFET Highway Fuel Economy Test (EPA)
MDS Multi-Displacement System
HC hydrocarbon
lambda excess air factor (AFR/stoichiometric AFR)
kPa kilopascals (pressure unit)
OEM original equipment manufacturer
ORNL Oak Ridge National Laboratory
SI spark ignition
SS steady speed
stoichiometric AFR AFR at which complete combustion would produce
only carbon dioxide and water (no excess fuel or
excess air)
THC total hydrocarbons
WOT wide-open throttle
vii
ACKNOWLEDGEMENTS
This report and the work described were sponsored by the U.S. Department of Energy (DOE) Office of
Energy Efficiency and Renewable Energy Vehicle Technologies Program. The authors gratefully
acknowledge the support of Dennis Smith and Kevin Stork at DOE. Several Oak Ridge National
Laboratory staff made important contributions to this work, including Bob Boundy, Robert Gibson, Ron
Graves, David Greene, Janet Hopson, Ron Lentz, Larry Moore, Scott Sluder, and John Thomas. The
authors also wish to thank Donnie Baldwin at Honeywell, John Hoard at the University of Michigan, and
Coleman Jones at General Motors for their thorough review and constructive recommendations. While
these experts provided valuable guidance and information as noted above, this does not constitute
endorsement by their organizations of either the study or the results. Grateful acknowledgement is also
due to V. J. Ewing and Sandi Lyttle for their dedication in preparation of the final manuscript.
ix
1. INTRODUCTION AND BACKGROUND
The U.S. Department of Energy (DOE) Office of Energy Efficiency and Renewable Energy and the U.S.
Environmental Protection Agency (EPA) jointly maintain a fuel economy website
(www.fueleconomy.gov), which helps fulfill their responsibility under the Energy Policy Act of 1992 to
provide accurate fuel economy information [in miles per gallon (mpg)] to consumers. The site provides
information on EPA fuel economy ratings for passenger cars and light trucks from 1985 to the present and
other relevant information related to energy use such as alternative fuels and driving and vehicle
maintenance tips. In recent years, fluctuations in the price of crude oil and corresponding fluctuations in
the price of gasoline and diesel fuels have renewed interest in vehicle fuel economy in the United States.
(User sessions on the fuel economy website exceeded 20 million in 2008 compared to less than 5 million
in 2004 and less than 1 million in 2001.) As a result of this renewed interest and the age of some of the
references cited in the tips section of the website, DOE authorized the Oak Ridge National Laboratory
(ORNL) Fuels, Engines, and Emissions Research Center (FEERC) to initiate studies to validate and
improve these tips. This report documents a study aimed specifically at the effect of engine air filter
condition on fuel economy.
A vehicle’s published EPA fuel economy rating is determined by driving the vehicle over prescribed
cycles on a chassis dynamometer. In the United States, city fuel economy is measured using the Urban
Dynamometer Driving Schedule, also known as the Federal Test Procedure (FTP). Highway fuel
economy is measured using the Highway Fuel Economy Test (HFET). Another relevant test is the US06,
an aggressive (high speed, high load) test used to confirm emissions compliance during aggressive
driving. Typically, fuel economy results from this test are not reported, but EPA uses them to adjust the
FTP and HFET results, and these adjusted fuel economy rates are what are reported on the vehicle
manufacturer’s window sticker, in the Fuel Economy Guide,1 and on the fueleconomy.gov website.
Vehicle design, including mass, rolling resistance, aerodynamic drag, and engine and transmission
efficiency, is an important factor affecting a vehicle’s fuel economy on the prescribed driving schedules.
Fuel economy can also be greatly affected by driver/owner behavior. Hard acceleration, excessive idling,
and carrying unnecessary weight can all negatively affect fuel economy. Proper vehicle maintenance, on
the other hand, can help the vehicle perform as it was designed, thus positively affecting fuel economy,
emissions, and the overall drivability of a vehicle.
The study described in this report investigates the effect of one of these maintenance factors, air filter
replacement, on vehicle performance and fuel economy. Past studies have indicated that replacing a
clogged or dirty air filter can improve vehicle fuel economy. For example, Jaroszczyk, Wake, and Connor
reported in 1993 that proper filtration systems make engines more fuel efficient; however, they gave no
data or reference information to support this claim.2 The Organization for Economic Co-operation and
Development claimed in a 1981 report based on earlier research by the Thornton Research Center that
“excessive pressure across a dirty air filter” can cause a 1–15% increase in fuel consumption.3 In the
Thornton study, six 1970–73 model year vehicles were tested using the Economic Commission for
Europe hot-start driving cycle (ECE 15) to explore the fuel economy effects of “deliberate malfunctions,”
defined as maintenance problems such as damaged spark plugs, poor idle mixture, improper idle speed,
and “restricted air cleaners.”4 Of the six vehicles, only five were tested with restricted air filters,
accomplished by “masking the cross-sectional area of the air cleaner element.”4 No further description of
how the amount of restriction was quantified was given, but the vehicles showed a variable response to
the testing. Two of the vehicles showed less than a 1% decrease in fuel economy, two others showed 11%
and 15% decreases in fuel economy, and the fifth vehicle showed a decrease in fuel economy of more
than 30% due to the restricted air cleaner.4 The Thornton researchers believed that this large change was
due to the style of carburetor used in this 1971 Vauxhall Viva, which utilized a fixed-jet atmospherically
1
2
vented carburetor, believed by the researchers to be very sensitive to a throttled air intake.4 The wide
variability in the effect of restricted air intake from a simulated clogged air filter was attributed to the
different styles of carburetors, which varied among the tested vehicles.4
The results of the Thornton Research Center tests are of limited use to consumers today because the
vehicle engine technology has evolved significantly since those tests were conducted. As of the early
1980s, some form of closed-loop fuel control had been implemented on most U.S. light-duty vehicles to
enable them to meet the EPA Tier 0 emissions standards. The authors hypothesized that the fuel economy
of modern closed-loop feedback systems would not be sensitive to the state of the air filter, given that the
engine power is controlled by throttling the intake air. Because of this, at a given engine power condition
(or given manifold pressure) additional throttling from a clogged air filter would be offset by further
opening the throttle (to achieve the same manifold pressure); however, maximum engine power would be
expected to be affected by the intake air restriction imposed by a clogged filter. While the authors
hypothesized that the fuel economy of modern engines would not be affected by a clogged filter, we
further hypothesized that a clogged filter might impact a carbureted engine due to a “choking effect” in
which the engine operates at richer combustion conditions.
This report describes a DOE-funded investigation into the effects of clogged air filters on the fuel
economy of three modern vehicles, ranging from 2003 to 2007, that use closed-loop fuel control and a
vintage 1972 vehicle equipped with a carburetor. The objectives of the program included
• determining the effects of clogged air filters on the fuel economy and performance of modern
vehicles,
• confirming the results of previous studies indicating that clogged filters affect the fuel economy of
carbureted or open-loop control vehicles, and
• determining other vehicle performance impacts of clogged filters (e.g., the potential impacts on
engine power).
2. EXPERIMENTAL SETUP
2.1 TEST FACILITIES
Testing was conducted at the ORNL FEERC. The FEERC chassis dynamometer is of the twin-roll type
[21.625-inch (0.55-meter) diameter] with an eddy current brake. Conventional emissions measurements
were conducted with analyzers from California Analytical Instruments. Nondispersive infrared sensors
were used to measure carbon dioxide (CO2) and carbon monoxide (CO), and heated chemiluminescence
detectors were used to measure nitrogen oxides (NOx). Total hydrocarbons (THC) and methane were
measured with a heated flame ionization detector with a methane cutter. Fuel economy was calculated
from the integrated “bag” emissions from the constant-volume dilution tunnel according to EPA and Code
of Federal Regulations guidelines. In this method, total carbon in the exhaust from the measured CO2,
CO, and THC emissions is used to compute fuel economy. The fuel used in all vehicles for all tests was
Federal Certification Gasoline with known carbon fraction and density for computing fuel economy.
Reported fuel economies are raw or unadjusted results, not directly comparable to window sticker or Fuel
Economy Guide1 values.
2.2 TEST SETUP
The vehicles tested included the following.
• 2007 Buick Lucerne—3.8L V6.
• 2003 Toyota Camry—2.4L I4.
• 2006 Dodge Charger—5.7L V8 with MDS (Multi-Displacement System).
• 1972 Pontiac Grandville—455ci V8 with factory four barrel carburetor.
For each of the three modern vehicles, three different pressure differentials (DPs) were measured on the
engine along with lambda excess air factor [nondimensional air : fuel ratio (AFR)] and tunnel emissions.
The DPs measured were as follows (see also Fig. 2.1).
• Inlet DP—The pressure differential between the area just before the air filter and the atmosphere.
• Filter DP—The pressure differential between the area just before the air filter and the area just after
the air filter.
• Outlet DP—The pressure differential between the area just after the air filter and the atmosphere.
These pressures were measured using three separate electronic delta P pressure transducers. Each
transducer was able to measure 0 to 7.5 kPa (0 to 30 inches of water column). The sensors were calibrated
before testing began using a water manometer. In a few experiments, the measured pressures exceeded
the range of these sensors. This issue did not present itself as a significant problem until late in testing
when “severe” test cases were explored (Sect. 3).
The Outlet DP measured was used to quantify the amount of restriction that was being added to the intake
system by the “clogged filter.” This pressure is the same pressure that is monitored by factory original
equipment manufacturer (OEM) air filter indicators such as the one shown in Fig. 2.2. These filter
indicators are used in some applications to alert the owner/operator when the air filter is in need of
replacement. In most cases the Filter DP measurement and the Outlet DP measurement were nominally
the same. Only the Outlet DP will be reported here as this is the value that a factory-installed indicator
would measure.
3
Fig. 2.1. Pressure transducer setup for modern vehicles.
Fig. 2.2. Air filter indicator.
A factory OEM indicator was taken from a 2001 Chevrolet Silverado with 5.3L V8 and tested to find the
Outlet DP required to “set” the indicator or move the yellow indicator into the red zone (see Fig. 2.2).
Using a vacuum pump and water manometer to test the indicator, the authors determined that an Outlet
DP of about 5.7 kPa was needed to set the indicator to the level corresponding to a clogged air filter.
Other air filter indicators from diesel applications were also tested. Both of the other two air filter
indicators tested were factory equipment for Dodge Ram pickup trucks with 5.9L diesel engines. One was
purchased new from the Chrysler dealer and the other was taken from a 2006 Dodge Ram pickup
equipped with a 5.9L diesel engine. Using the same vacuum pump and water manometer, the authors
4
found that the vacuum needed to set these indicators was slightly less than that required by the indicator
taken from the gasoline application. These air filter indicators only required about 4.2 kPa to move the
indicator to the level corresponding to a clogged air filter. Tests of diesel vehicles are planned as a follow-
on effort to the work reported here.
2.3 DEFINING A CLOGGED AIR FILTER
The results of the testing of these air filter indicators agreed with the information found in the literature as
to what the definition of a clogged air filter is in engineering terms. The function and design of intake air
filters must address the following.5
1. Engine durability
2. Filtration
3. Flow management
4. Pressure or head loss constraints
5. Overall noise, vibration, and harshness standards
6. Service requirements
7. Packaging
8. Styling/appearance
9. Emissions
All of these functions are to be met for the service life of the filter without allowing engine performance
to be affected.5 In light- and medium-duty applications, the service life is normally defined by
accumulated mileage. However, it is very common for over-servicing to occur in these applications due to
a lack of understanding of how optimum air filter efficiency is achieved.5,6 The standard recommended
service life for an air filter in light- and medium-duty applications, during normal driving conditions, is
about 30,000 miles.5–7 It is common, however, for servicing to occur when the filter appears dirty. Engine
air filters are designed to actually increase their efficiency by using this initial layer of dust as an added
filter layer. Initial filter efficiency is usually approximately 98% but increases to more than 99% by the
end of the service life of the filter.7,8 Therefore, changing an air filter before the useful service life is
achieved can result in premature engine wear.6,9
In engineering terms, the service life of an air filter is commonly defined as a level of restriction which
results in a pressure drop across the filter of approximately 2.5 kPa (10 in. water) more than the pressure
drop of the new or clean filter.5,9–11 Bugli and Green define this as the “final pressure drop” when
conducting tests to investigate filter cleaning procedures:
Final pressure drop = initial clean pressure drop + 2.5 kPa.10
According to Patil, Halbe, and Vora, it is common for air filter service indicators to be set between about
5.0 and 7.0 kPa, which corresponds to the setting of the unit taken from the Chevrolet Silverado. The unit
tested from the 2006 Dodge Ram is set at a slightly lower level, which is believed to be due to the vehicle
being equipped with a diesel engine. While the level of restriction on a closed-loop, feedback, throttled,
spark-ignition (SI) engine would not be expected to affect fuel economy (as described above), the
additional pumping loss might be expected to affect the fuel economy of the unthrottled diesel engine.
This restriction level is noted as the point of critical pressure drop because at levels greater than the “final
pressure drop,” overall engine performance begins to degrade significantly.5,7,8,11
5
2.4 VEHICLE TESTING
Wide-open throttle (WOT) tests were used to measure the changes in the filter pressure drop (Outlet DP).
In a real-world application, the vacuum needed to set one of the air filter indicators would likely occur
under heavy acceleration, such as merging onto an interstate, or climbing a steep grade. Therefore the
level of restriction was set, using an artificial clogging technique described below, to achieve the desired
Outlet DP during a WOT acceleration from idle to approximately 85 mph or a steady-speed (SS) WOT
test in which the dynamometer was held at a fixed speed, 65 mph, and the throttle was held open for
10 seconds. Using these test procedures, the 2007 Buick Lucerne was configured to achieve an Outlet DP
of approximately 7.0 kPa under the WOT acceleration and approximately 5.7 kPa under the SS WOT.
Once the method for achieving this restriction was developed, it was used with each vehicle. Using this
approach, the V8-equipped Dodge Charger showed a slightly higher Outlet DP than the V6 Lucerne, and
the I4 Camry showed a slightly lower Outlet DP. The 1972 V8 Pontiac was restricted in a similar manner
and level. It is important to note that all the modern vehicles used rectangular cartridge style air filters
(Figs. 2.3 and 2.4), while the 1972 Pontiac used the cylindrical filter element common in that era
(Fig. 2.5).
For all of the vehicles, a warm-up test was run before starting the WOT cycles. The warm-up cycle
consisted of 5 minutes at 50 mph followed by 3 minutes at 30 mph. This 8-minute warm-up was always
conducted on a warm engine (i.e., the engine had been run earlier that day). The acceleration WOT tests
were run first, followed by the SS WOT tests. Five of each WOT test were conducted. The acceleration
WOT tests used a procedure known as the modified Coordinating Research Council (CRC) E-60
protocol.12 The SS WOT tests were run by slowly accelerating the vehicle to approximately 65 mph,
where the dynamometer control was set to hold a fixed speed. Once the vehicle speed reached 65 mph,
the operator held this cruise condition for 10 seconds then opened the throttle to the WOT position for
another 10 seconds. The vehicle was then brought back to idle for 30 seconds, and the process was
repeated.
In all cases, the “new” air filter was a newly purchased aftermarket filter for that specific application. The
simulated clogged air filter was another identical filter that was blocked off with a series of disposable
shop towels to create the desired pressure drop. For the newer vehicles, the shop towels were placed in the
air box on the upstream side of the air filter to increase the resistance of the air flowing through, as shown
in Figs. 2.3 and 2.4. In the case of the 1972 Pontiac, the round filter was wrapped with shop towels to
create the desired resistance, as shown in Fig. 2.5. Before the procedure for simulating a clogged filter
was established, several filters were tested on the 2007 Buick. The OEM air filter was found to have a
slightly higher pressure drop at WOT than several aftermarket air filters. The aftermarket filters were used
for this testing to generate the largest difference between “clean” and “clogged” for these experiments.
Other methods of restriction were considered before we decided upon the use of shop towels. The idea of
using an orifice plate was decided against due to the fear of not having a consistent restriction across a
range of flow rates or engine speeds. Loading the filter with particles such as soil or flour was not
considered to be repeatable or feasible due to the handling issues that would result. Taping off sections of
the filter could be used to accomplish the desired pressure drop; however, this approach would not result
in uniform restriction across the full area of the filter. In addition, completely blocking off sections of the
filter could affect the flow dynamics of the inlet system. Paint was also considered but rejected due to
drying time, the inability to reduce pressure drop if set too high, and the potential for undesirable HC
emissions. Thus the use of shop towels was adopted to generate a repeatable air filter pressure drop.
After establishing the WOT test procedure for quantifying the filter state, the standard EPA test cycles,
FTP, HFET, and US06 (see Sect. 1.1), were run in triplicate to test for fuel economy or emissions effects.
6
Fuel economy values reported for the HFET and US06 are from the second of the two cycles. For both
cycles, common practice is to conduct the cycle twice, reporting only the data from the second cycle.
Fig. 2.3. 2007 Buick Lucerne filter restriction. Shop towels inserted into air box
upstream of the air filter.
Fig. 2.4. 2007 Buick Lucerne filter restriction. Shop towels inserted into air box
upstream of the air filter.
7
8
Fig. 2.5. 1972 Pontiac Grandville air filter. Filter on the left shows damage that
occurred during “severely clogged” filter testing (see Sect. 3.3.1).
3. RESULTS AND DISCUSSION
3.1 MODERN VEHICLES
3.1.1 Initial Testing
Four filter setups, an OEM filter, an aftermarket filter, a performance aftermarket filter, and no filter,
were tested, using the 2007 Buick Lucerne as the test vehicle, to determine a baseline and the filter to be
used for the remainder of the testing. Each setup was tested over the WOT cycle described previously. It
was observed that the OEM filter resulted in a higher Outlet DP than the aftermarket filter and the
performance aftermarket filter, as is shown in Fig. 3.1. The aftermarket filter was chosen for the test
process due to its lower initial Outlet DP compared to the OEM filter and because it is more common than
the performance aftermarket filter; thus, it allowed us to explore the largest clean-to-clogged difference
for a commonly used air filter. No measureable differences were observed in vehicle performance with
these filters over the CRC E-60 WOT test cycle.
1.56
1.07
0.88 1.11
0.0
0.2
0.4
0.6
0.8
1.0
1.2
1.4
1.6
1.8
2.0
No Filter Aftermarket
Performance Filter Aftermarket Filter OEM Style Filter
Pressure Drop (kPa)
Fig. 3.1. Maximum Outlet DP for 2007 Buick Lucerne baselined clean air
filters. Initial testing done to baseline multiple clean air filters.
3.1.2 WOT Testing
Each of the three newer vehicles listed in Sect. 2.2 was tested in the same manner to compare the effects
of a clean versus a clogged filter. The vehicles are shown in Fig. 3.2. Each vehicle was instrumented with
the electronic delta P pressure transducers reading Inlet DP, Filter DP, and Outlet DP during testing. The
restriction level was initially set using the 2007 Buick Lucerne, equipped with a 3.8L V6, such that the
maximum Outlet DP was about 7.0–7.2 kPa during the CRC E-60 WOT tests and about 5.7–6.0 kPa
during the SS WOT tests. Both conditions would allow for a common air filter indicator to be set,
indicating to the user that the vehicle’s air filter should be changed. Once the restriction level was
determined, the same number and style of disposable shop towels were used for each vehicle to simulate a
similar degree of clogging. This approach resulted in a slight variance of the Outlet DP depending on the
9
vehicle due to differences in filter area and engine displacement. In all cases the restriction was on the
order of 6.0–7.0 kPa, adequate to set a common air filter indicator.
Fig. 3.2. Newer vehicles tested.
2007 Buick Lucerne
2003 Toyota Camry
2006 Dodge Charger
For the 2003 Camry, which was equipped with a 2.4L I4, the clogged filter created an Outlet DP in excess
of 6.2 kPa for the CRC E-60 WOT tests (Fig. 3.3), while the new filter produced less than 1.7 kPa under
the same acceleration conditions. For the SS WOT tests (Fig. 3.4), the clogged filter created an Outlet DP
in excess of 4.2 kPa, while the new filter generated approximately 0.5 kPa under the same acceleration
conditions. The data in Fig. 3.3 represent the Camry’s average maximum Outlet DP recorded for the
WOT accelerations during the CRC E-60 WOT section of the test.
For the 2006 Dodge Charger, which was equipped with a 5.7L V8 with MDS, the clogged filter resulted
in an increase of the Outlet DP compared to the Lucerne. The Charger testing resulted in a maximum
Outlet DP in excess of 7.5 kPa for the CRC E-60 WOT tests and approximately 7.2–7.5 kPa for the SS
WOT tests. The MDS is Chrysler’s cylinder deactivation system. This system disables the intake and
exhaust valves and fuel delivery for four cylinders during low-load operation to reduce pumping losses
and improve part-load fuel economy. This system was monitored during testing by collecting fuel injector
pulse width data from two injectors, one which is intermittently deactivated by the MDS and one which is
not.
10
1.58 6.71
0
1
2
3
4
5
6
7
8
Toyota Camry
(Max)
Pressure Drop (kPa)
New Air Filter
Clogged Air Filter
Fig. 3.3. Average maximum Outlet DP for the 2003 Toyota Camry during the CRC
E-60 WOT tests.
0.30 1.02 6.284.10
0
1
2
3
4
5
6
7
8
Buick Lucerne
(3000 RPM) Dodge Charger
(3000 RPM)
Pressure Drop (kPa)
New Air Filter
Clogged Air Filter
Fig. 3.4. Average Outlet DP at 3000 RPM during the CRC E-60 WOT tests.
Because the peak Outlet DP for the Charger and Lucerne were outside the range of the sensor in the
clogged state, the average of the Outlet DPs at 3000 RPM, recorded for each of the WOT accelerations
11
during the CRC E-60 WOT section of the test, was used to compare these vehicles, as shown in Fig. 3.4.
The Outlet DP values for the SS WOT tests were all within the range of the sensor and are shown in
Fig. 3.5.
1.13
0.80
0.50 7.40
5.92
4.28
0
1
2
3
4
5
6
7
8
Toyota Camry Buick Lucerne Dodge Charger
Pressure Drop (kPa)
New Air Filter
Clogged Air Filter
Fig. 3.5. Average maximum Outlet DP for SS WOT tests.
For the Lucerne, the Outlet DP at 3000 RPM during the initial acceleration of the CRC E-60 WOT tests
was in excess of 4 kPa for the clogged filter and less than 0.4 kPa for the new filter (Fig. 3.4). During the
SS WOT tests the clogged filter created an Outlet DP in excess of 5.7 kPa, while the new filter Outlet DP
was less than 0.9 kPa (Fig. 3.5).
For the Charger, the Outlet DP at 3000 RPM during the initial acceleration of the CRC E-60 WOT tests
was in excess of 6.2 kPa for the clogged filter, while that for the new filter was less than 1.1 kPa under the
same acceleration conditions (Fig. 3.4). During the SS WOT tests the clogged filter created an Outlet DP
in excess of 7.2 kPa, while the new filter Outlet DP was less than 1.2 kPa under the same acceleration
conditions (Fig. 3.5).
Also, for the Charger, under these acceleration conditions with the filter clogged, the pressure drop was so
severe that the air filter was actually dislodged from its position in the air cleaner box and pulled into the
intake hose. Fig. 3.6 shows the damage that was done to the air filter as a result of these clogged air filter
WOT tests.
Figure 3.7 shows the acceleration times for the vehicles with both a clogged and new air filter. The data
were analyzed from 20 to 80 mph to ensure that the vehicle was at WOT, removing any driver induced
variability. The WOT protocol requires the vehicle to be accelerated at WOT from idle to 85 mph. The
driver reported being able to “feel” the restriction created by the clogged filter and sense the decreased
acceleration for both the Camry and Lucerne. The Charger was 0.6 seconds slower in the clogged state,
but the driver reported no noticeable decrease in acceleration.
12
Fig. 3.6. Air filter damage from WOT testing 2006 Dodge Charger. Filter was
damaged due to the pressure drop across the filter, resulting in the filter being torn out
of its seat in the air box.
10.23
13.77
17.24 10.84
15.45
18.51
0
2
4
6
8
10
12
14
16
18
20
Toyota Camry Buick Lucerne Dodge Charger
Time (s)
New Air Filter Clogged Air Filter
*
Acceleration times are
from 20 to 80 MPH at WOT.
1.26 sec or 7%
1.68 sec or 11%
0.61 sec or 6%
Fig. 3.7. Acceleration time for CRC E-60 WOT tests. Data are averaged from
the five accelerations of the CRC E-60 cycle.
13
3.1.3 Performance and Fuel Economy
The simulated clogged filter significantly affected vehicle performance, increasing the time to accelerate
from 20 to 80 mph by 0.6 to 1.7 seconds on the three vehicles. The Outlet DP measured for each vehicle
was sufficient for setting a common air filter indicator to the “change” or “clogged” position. For each
vehicle, the Outlet DP at some point exceeded 5 kPa and showed an increase over the clean filter in
excess of 2.5 kPa, a common standard for defining a dirty air filter.5,9–11
Despite the filter restrictions, however, no significant changes in fuel economy were observed. Each
vehicle was run through at least three rounds of FTP, HFET, and US06 tests with the new air filter, and
the same protocol was repeated with the clogged air filter. The tests were conducted on consecutive days
for each vehicle. This format was used to allow for the required soak time to perform a cold FTP each
morning. The resulting fuel economy data for the vehicles are shown in Figs. 3.8, 3.9, and 3.10. Range
bars in the figures show the minimum and maximum of the tests for each case, while the columns show
the average. Test-to-test repeatability is within about 1.5%, and all of the variances between the new and
clogged air filter cases are similarly within about 1.7%. The baseline fuel economies for the vehicles were
all within 0–6% of unadjusted EPA certification database values (www.epa.gov) for similar vehicles.
The changes observed by clogging the air filter produced no significant effect on the fuel economy of the
vehicles tested, when tested over these three standard cycles that represent a wide range of driving
conditions. It is possible that there may be some isolated operating conditions under which the fuel
economy may be more susceptible to a clogged air filter. However, such operating conditions are not
likely to be consistent from vehicle to vehicle. The three driving cycles used here are representative of a
wide range of driving conditions, as described in Sect. 1.
25.1
39.4
25.2 25.3
39.4
25.2
15
20
25
30
35
40
FTP HFET US06
Fuel Economy (mpg)
New Air Filter
Clogged Air Filter
No Measured
Difference
No Measured
Difference
0.9%
Fig. 3.8. Fuel economy for 2003 Toyota Camry. Data are averaged over the three
tests conducted for each cycle and configuration. Range bars show the minimum and
maximum for each data set.
14
22.9
35.9
20.0 22.8
36.5
20.2
15
20
25
30
35
40
FTP HFET US06
Fuel Economy (mpg)
New Air Filter
Clogged Air Filter
1.7%
1.1%
0.5%
Fig. 3.9. Fuel economy for 2007 Buick Lucerne. Data are averaged over the four tests
conducted for each cycle and configuration. Range bars show the minimum and maximum for
each data set.
18.4 32.2 20.6
18.2 32.6 20.8
15
20
25
30
35
40
FTP HFET US06
Fuel Economy (mpg)
New Air Filter
Clogged Air Filter
1.4%
0.9%
0.8%
Fig. 3.10. Fuel economy for 2006 Dodge Charger. Data are averaged over the three tests
conducted for each cycle and configuration. Range bars show the minimum and maximum for
each data set.
15
3.2 CARBURETED VEHICLE—1972 PONTIAC GRANDVILLE
To investigate the effect of a clogged air filter on a carbureted engine, a 1972 Pontiac Grandville with a
455ci V8 engine was also tested (Fig. 3.11). The Pontiac was only instrumented with the electronic delta
P pressure transducer reading the Outlet DP during testing, configured so that it measured the pressure
after the air filter and referenced that to the ambient air pressure. This setup is shown in Fig. 3.12.
Fig. 3.11. 1972 Pontiac Grandville.
Fig. 3.12. Pressure port location for 1972 Pontiac Grandville.
16
The restriction level was set in the same manner as for the other vehicles. The shop towels were cut and
taped to the outside of the round air filter used by the Pontiac. This setup was used to correlate with the
restriction that was applied to the other vehicles. The WOT cycles were both decreased from five
accelerations to three accelerations each to minimize wear and tear on this vintage vehicle. During the
CRC E-60 WOT accelerations and during the SS WOT tests, the maximum Outlet DP exceeded the range
of the sensor. Both conditions would allow for a common air filter indicator to be set, indicating to the
user that the vehicle’s air filter should be changed.
Also, under these acceleration conditions with the filter clogged, the pressure drop was so severe that the
air filter was crushed slightly in one area.
The Outlet DPs for the new filter and simulated clogged filter from the CRC E-60 WOT and SS WOT
tests are shown in Figs. 3.13 and 3.14. The peak Outlet DP for the clogged filter is in excess of 7.5 kPa
for the CRC E-60 WOT—the sensor is at its maximum range for each of the accelerations—while that for
the new filter is less than 0.75 kPa under the same acceleration conditions. For the SS WOT tests, the
clogged filter again showed an Outlet DP in excess of 7.5 kPa, while the new filter again showed less than
0.75 kPa under the same acceleration conditions. These results can be considered analogous to the Filter
DP because the sensor was reading the post-filter pressure versus the ambient pressure. This means that,
in both WOT cases, the clogged filter was exhibiting a pressure drop greater than 7.5 kPa across the air
filter. Because of time constraints, we proceeded with testing rather than waiting to procure a sensor with
a larger range.
0
1
2
3
4
5
6
7
8
9
10
400 450 500 550 600
Time (s)
Pressure Drop (kPa)
Clogged Air Filter
New Air Filter
Fig. 3.13. Outlet DP for 1972 Pontiac Grandville during CRC E-60 WOT.
17
0
1
2
3
4
5
6
7
8
9
10
1100 1150 1200 1250 1300
Time (s)
Pressure Drop (kPa)
Clogged Air Filter
New Air Filter
Fig. 3.14. Outlet DP for 1972 Pontiac Grandville during SS WOT.
Figure 3.15 shows that in the clogged filter scenario, the average time it took to accelerate from 20 to
80 mph during the WOT tests increased by about 3.73 seconds or 23%. The driver reported a noticeable
loss of performance during the WOT testing with the simulated clogged filter.
0
2
4
6
8
10
12
14
16
18
20
New Air Filter Clogged Air Filter
Time (s)
Acceleration time from 20 to 80 MPH is
3.73 sec lon
g
er with the clo
gg
ed filter.
Fig. 3.15. Acceleration time for 1972 Pontiac Grandville during WOT tests.
Data are averaged over the three CRC-E60 accelerations from 20 to 80 mph with the
throttle at 100%. Range bars show the minimum and maximum for each data set.
The Pontiac was run through three rounds of FTP and HFET tests with the new air filter, and the same
protocol was repeated with the clogged air filter. The US06 tests were not conducted after two failed
18
attempts to complete that cycle with this vehicle. The US06 cycle requires aggressive accelerations and
has extended periods of high speed operation (up to 80 mph). The 1972 Pontiac overheated during these
high speed sections of the US06. Therefore, to avoid damaging the vehicle, the US06 tests were not
conducted. The FTP and HFET tests were conducted on consecutive days, with each test being run once
per day, similar to the other vehicles. This format was used to allow for the required soak time to perform
a cold FTP each morning. The resulting fuel economy data for the Pontiac are shown in Fig. 3.16. Test-to-
test repeatability is within about 1.8% for the Pontiac, and the new versus clogged cases show a drop of
about 2%–2.5%. The level of filter clog tested appears to have a small effect on the fuel economy of this
carbureted vehicle although it is not as dramatic as some of the fuel economy differences reported in the
literature.3
11.1 17.7
10.9 17.3
0
5
10
15
20
FTP HFET
Fuel Economy (mpg)
New Air Filter
Clogged Air Filter
2.1%
2.5%
Fig. 3.16. Fuel economy for 1972 Pontiac Grandville. Data are averaged over the
three tests conducted for each cycle and configuration. Range bars show the minimum
and maximum for each data set.
3.3 FURTHER INVESTIGATIONS—SIMULATING A SEVERELY CLOGGED FILTER
3.3.1 1972 Pontiac Grandville
While the filter restriction tested was severe enough to exceed 7.5 kPa at WOT, it is conceivable that
some consumers never experience WOT and could allow their filters to become even more severely
clogged. In the interest of validating the large fuel economy penalties noted in the literature, further
testing was conducted to investigate more severely clogged cases. The level of restriction was increased
in stages to allow quantification of the maximum tolerable restriction that would still allow the vehicle to
meet the HFET cycle. These increases were tested and quantified using the normal double HFET test
procedure. The level of restriction was increased in three stages or tests until the vehicle was barely able
to meet the required speed for the test. The average Outlet DPs measured over the double HFET for these
three severely clogged filter tests are shown in Fig. 3.17 with the Outlet DPs for the originally tested
clogged filter and new air filter.
19
0.01
5.05
1.84
3.19
5.96
0
1
2
3
4
5
6
7
8
9
10
New Air Filter Clogged Air
Filter Severely
Clogged Air
Filter Test 1
Severely
Clogged Air
Filter Test 2
Severely
Clogged Air
Filter Test 3
Pressure Drop (kPa)
Fig. 3.17. Air filter average Outlet DPs for 1972 Pontiac
Grandville during double HFET.
The filter restriction in the Severely Clogged Air Filter Test 3 configuration (black column, Fig.3.17) was
so severe that the driver had to consciously drive the vehicle in a manner that would not increase the
throttle fast enough to cause a rich misfire condition during the HFET cycle. Once rich misfire was
encountered, the vehicle was not able to maintain speed, and therefore, the test was invalid. The Filter
Test 3 configuration also resulted in the air filter being crushed by the air filter cover. Figure 3.18 shows a
picture of the air filter after removal of the shop towels.
Fig. 3.18. Damaged air filter from severely clogged air filter testing, 1972
Pontiac Grandville.
20
For each of the tests simulating severely clogged filters, fuel economy was calculated for the FTP and
HFET cycles. However, due to the nature of the cold FTP tests that were being conducted, time
constraints did not allow for the vehicle to be prepared for a cold FTP for the Severely Clogged Air Filter
Test 1 setup. Each incremental increase in restriction resulted in an incremental decrease in fuel economy
for the HFET, but FTP fuel economy was not affected as severely by the restriction. Figure 3.19 shows
the FTP fuel economy for the different stages of testing. Figure 3.20 shows the same information for the
HFET.
11.13 10.30
10.30
10.90
0
2
4
6
8
10
12
New Air Filter Clogged Air
Filter Severely
Clogged Air
Filter Test 1
Severely
Clogged Air
Filter Test 2
Severely
Clogged Air
Filter Test 3
Fuel Economy (mpg)
No Test Conducted
Fig. 3.19. FTP fuel economy for 1972 Pontiac Grandville.
15.18
16.26
16.81
17.73 17.28
0
2
4
6
8
10
12
14
16
18
20
New Air Filter Clogged Air
Filter Severely
Clogged Air
Filter Test 1
Severely
Clogged Air
Filter Test 2
Severely
Clogged Air
Filter Test 3
Fuel Economy (mpg)
Fig. 3.20. HFET fuel economy for 1972 Pontiac Grandville.
21
The initial change in fuel economy from the new air filter to the clogged air filter resulted in an FTP fuel
economy decrease of 2.1%. The HFET fuel economy initially decreased 2.5% from the new air filter to
the clogged air filter.
For Severely Clogged Air Filter Test 1, the HFET fuel economy decreased another 2.7% from the initial
clogged air filter test (a 5.2% decrease from the new filter case). The progression from the initial clogged
filter test and the Severely Clogged Filter Test 1 were on the same day, so no FTP data are available.
For Severely Clogged Air Filter Test 2, the restriction level was increased further to obtain a greater
Outlet DP resulting in an additional loss of fuel economy. Fuel economy under the FTP decreased more
than 5% from the initial clogged air filter test results and about 7.5% from the results for the new air filter.
The HFET data for Severely Clogged Air Filter Test 2 showed a fuel economy decrease of about 3% from
that in Filter Test 1 and more than 8% from that of the new air filter.
The restriction for Severely Clogged Air Filter Test 3 was so severe that the vehicle would not accelerate
past about 70–75 mph, and the driver had to consciously control the rate of change of the throttle to avoid
rich misfire conditions. The HFET, like all certification tests, requires that the vehicle be operated over a
defined cycle. If the vehicle is unable to meet the speed and acceleration requirements of the cycle, the
test is deemed invalid. The maximum speed of the HFET cycle is about 60 mph, and further restriction
would not allow the vehicle to meet the accelerations required during the cycle, invalidating the test.
Therefore, this level of restriction was determined as the maximum possible restriction that could be
tested. Figure 3.21 shows the average lambda (actual AFR divided by stoichiometric AFR) for the double
HFETs conducted. The severely clogged air filter results in a much richer AFR (lambda < 1 = rich,
lambda > 1 = lean). The trace file collected for the severely clogged filter test runs showed rich
excursions to nearly 0.60 lambda during some of the accelerations of the cycle.
1.03 1.01
0.96
0.93
0.86
0.80
0.85
0.90
0.95
1.00
1.05
1.10
New Air Filter Clogged Air
Filter Severely
Clogged Air
Filter Test 1
Severely
Clogged Air
Filter Test 2
Severely
Clogged Air
Filter Test 3
Excess Air Factor (lambda)
Fig. 3.21. Average double HFET lambda for 1972 Pontiac Grandville.
With the Test 3 configuration, the fuel economy did show a decrease similar to what was found in the
Thornton study.4 The FTP fuel economy did not show any further decrease compared to Severely
22
Clogged Air Filter Test 2, but the HFET fuel economy continued to decrease another 6% compared to
Test 2 and showed a 14.4% decrease compared to the new air filter.
3.3.2 2007 Buick Lucerne
After observing the effect of continuously increased restrictions on the fuel economy of the 1972 Pontiac,
the authors decided that a greater level of restriction should also be investigated on one of the newer
vehicles. Thus the 2007 Buick Lucerne was retested to explore the effects of a more severely clogged air
filter on its fuel economy. The approach was to clog the air filter so severely that the vehicle would barely
be able to follow the HFET cycle, similar to the final test of the Pontiac. This objective was not
achievable. Before that level of restriction could be reached, the filter was pulled out of its seat in the air
box due to the large pressure drop (Fig. 3.22). The average Outlet DP for the double HFET test is shown
in Fig. 3.23 as Severely Clogged Air Filter Test 1. With the filter being dislodged during the test, the
Severely Clogged Air Filter Test 1 data represent a test in which the air flow restriction was probably not
consistent for the entire test.
Fig. 3.22. Damaged air filter from severely clogged air filter testing, 2007 Buick
Lucerne.
Data were collected for another test in which the level of restriction was higher than previously tested but
not so high as to unseat the filter element. The Outlet DP related to this level of restriction is shown in
Fig. 3.23 as Severely Clogged Air Filter Test 2.
The Lucerne was only tested over the double HFET cycle for these severely clogged filter simulation
tests. The effects of the simulated severely clogged filter on the Lucerne’s fuel economy were not
significant—less than 2%. These values are within the range for the series of tests that were conducted
during the initial testing. Figure 3.24 shows the fuel economy of Severely Clogged Air Filter Test 1 and
Test 2 versus the new air filter over the HFET cycle. The Lucerne’s control system maintained a
consistent AFR (lambda = 1.0) in all the tests conducted, regardless of air filter condition.
23
24
0.50
2.09
0.003
1.85
0.0
0.5
1.0
1.5
2.0
2.5
3.0
New Air Filter Clogged Air Filter Severely Clogged
Air Filter Test 1 Severely Clogged
Air Filter Test 2
Pressure Drop (kPa)
Fig. 3.23. Air filter average double HFET Outlet DP for 2007 Buick Lucerne.
35.135.1 34.4
34.7
15
20
25
30
35
40
HFET/Test 1 HFET/Test 2
Fuel Economy (mpg)
New Air Filter
Clogged Air Filter
1.1% 1.8%
Fig. 3.24. Severely clogged air filter fuel economy for 2007 Buick Lucerne.
4. CONCLUSIONS AND FUTURE WORK
4.1 CONCLUSIONS
The goal of this study was to explore the effects of a clogged air filter on the fuel economy of vehicles
operating over prescribed test cycles. Three newer vehicles (a 2007 Buick Lucerne, a 2006 Dodge
Charger, and a 2003 Toyota Camry) and an older carbureted vehicle were tested.
Results show that clogging the air filter has no significant effect on the fuel economy of the newer
vehicles (all fuel injected with closed-loop control and one equipped with MDS). The engine control
systems were able to maintain the desired AFR regardless of intake restrictions, and therefore fuel
consumption was not increased. The carbureted engine did show a decrease in fuel economy with
increasing restriction. However, the level of restriction required to cause a substantial (10–15%) decrease
in fuel economy (such as that cited in the literature3,4) was so severe that the vehicle was almost
undrivable. Acceleration performance on all vehicles was improved with a clean air filter.
Once it was determined how severe the restriction had to be to affect the carbureted vehicle fuel economy,
the 2007 Buick Lucerne was retested in a similar manner. We were not able to achieve the level of
restriction that was achieved with the 1972 Pontiac with the Lucerne. The Lucerne’s air filter box would
not hold the filter in place under such severe conditions. (It is believed that this testing exceeded the
design limits of the air box.) Tests were conducted at a lower restriction level (although still considerably
more severe than the initial clogged filter testing), allowing the air filter to stay seated in the air box, and
no significant change was observed in the Lucerne’s fuel economy or the AFR over the HFET cycle.
Closed-loop control in modern fuel injected vehicle applications is sophisticated enough to keep a
clogged air filter from affecting the vehicle fuel economy. However for older, open-loop, carbureted
vehicles, a clogged air filter can affect the fuel economy. For the vehicle tested, the fuel economy with a
new air filter improved as much as 14% over that with a severely clogged filter (in which the filter was so
clogged that drivability was impacted). Under a more typical state of clog, the improvement with a new
filter ranged from 2 to 6%.
4.2 FUTURE WORK
Power in the modern SI engine is controlled by manipulating the manifold pressure through throttling of
the intake air. The increased restriction of a clogged filter affects ultimate power but not fuel economy of
modern SI engines. Any additional pumping loss due to the state of the air filter is offset by the throttle.
Conventional diesel engines operate without throttles—although throttles are in use in some diesels today
for active control of exhaust temperature and species, to enhance warm-up, or control exhaust gas
recirculation, these throttles are full open most of the time. Because the diesel engine is unthrottled, and
airflow is high even at light load, the added restriction from a clogged filter may have a measureable
effect on fuel economy. Future work will investigate the effect of intake air filter state on a number of
diesel vehicles.
25
5. REFERENCES
1. U.S. Department of Energy Office of Energy Efficiency and Renewable Energy/U.S. Environmental
Protection Agency, Fuel Economy Guide, DOE/EE-D325.
2. Jaroszczyk, T., J. Wake, and M. J. Connor, “Factors Affecting the Performance of Engine Air
Filters,” Journal of Engineering for Gas Turbines and Power, 115, pp. 693–699 (October 1993).
3. Organization for Economic Co-operation and Development (OECD), Automobile Fuel Consumption
in Actual Traffic Conditions (OECD, Paris, December 1981) pp.74–78.
4. Atkinson, J., and O. Postle, “The Effect of Vehicle Maintenance on Fuel Economy,” in D. R.
Blackmore and A. Thomas, Fuel Economy of the Gasoline Engine (Shell Research Limited,
Thornton Research Center, Chester, United Kingdom, 1977).
5. Bugli, Neville J., Automotive Engine Air Cleaners—Performance Trends, Society of Automotive
Engineers Technical Series 2001-01-1365.
6. Grafe, Timothy, et al., “Nanofibers in Filtration Applications in Transportation,” International
Conference and Exposition of the INDA (Association of the Nonwovens Fabric Industry), Chicago,
Illinois, December 3–5, 2001.
7. Patil, A. S., V. G. Halbe, and K.C. Vora, A System Approach to Automotive Air Intake System
Development, Society of Automotive Engineers Technical Series 2005-26-011.
8. Zemaitis, Wally, “Stacked Panel Filter for Engine Air Intake Systems,” International Congress and
Exposition, Detroit, Michigan, February 23–36, 1998, Society of Automotive Engineers Technical
Series 980868.
9. Bugli, Neville J., and Gregory S. Green, “Performance and Benefits of Zero Maintenance Air
Induction Systems,” 2005 SAE World Congress, Detroit, Michigan, April 11–14, 2005, Society of
Automotive Engineers Technical Series 2005-01-1139.
10. Bugli, Neville J., Scott Dobert, and Scott Flora, “Investigating Cleaning Procedures for OEM
Engine Air Intake Filters,” 2007 World Congress, Detroit, Michigan, April 16–19, 2007, Society of
Automotive Engineers Technical Series 2007-01-1431.
11. Thiyagarajan, P, and V. Ganesan, “Study of Flow through Air Filter for Off Highway Vehicle—A
Preliminary CFD Approach,” Society of Automotive Engineers Technical Series 2005-26-339.
12. West, Brian, et al., Effects of Intermediate Ethanol Blends on Legacy Vehicles and Small Non-Road
Engines, Report 1, ORNL/TM-2008/117, October 2008.
27